Analysis of the Fracture Failure of ST90 Coiled Tubing
DOI:
https://doi.org/10.62051/ijcsit.v5n1.24Keywords:
Coiled tubing, Hardness test, Metallographic analysis, FractureAbstract
This article determines the causes of fracture failure of the ST90 coiled tubing through chemical composition analysis, dimensional measurement, metallographic analysis, and hardness testing of the fractured tubing sample. The material test results show that the chemical composition, size, grain size and hardness test results of the fractured coiled tubing meet the standard requirements, and no abnormal results are found. There is mechanical trauma in the fracture and suspected improper operation on both sides of the fracture position, which causes the tube body damage by the stacking of the clamping blocks, that will cause the deformation of the coiled tubing. The thinning of the wall thickness and the increase of hardness will reduce the strength of the tubing, which is the main reason for the fracture of the coiled tubing.
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[1] Zhao Jinlan, Cheng Pei, Wang Bin, et al. Fracture Failure Analysis of TS - 90 Coiled Tubing [J]. Welded Pipe and Tube, 2022, 45(06): 39 - 44. DOI: 10.19291/j.cnki.1001 - 3938.2022.06.007.
[2] Wang Weidong, Wang Liang, Wang Chao, et al. Failure Analysis of Coiled Tubing [J]. Chemical Equipment Technology, 2023, 44(02): 45 - 48. DOI: 10.16759/j.cnki.issn.1007 - 7251.2023.04.012.
[3] Tang Guoping. Research on Low - Cycle Fatigue Characteristics and Life Prediction of CT90 Coiled Tubing [D]. China University of Petroleum (Beijing), 2017.
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